Oh, and also while trying (and failing) to search for something on the I Roll facebook page, I stumbled across a post where my car was spotto'd:

Image description

I think this might've been while we were roadtripping over from Adelaide, and it was in Williamstown, and it was a hot as balls day (22nd December 2022), and after driving off from there was when I stalled the car and was glad I'd fixed the hot-start issue. Drove through the burnley tunnel after that and the car was really pushing the temps stuck in a tunnel in gridlock late in the afternoon… seared into my memory. Looks alright in the photo tho 😃

2 months later

March 2024 - Dump pipe

After a lengthy roadtrip in January, I noticed there was a very obvious exhaust leak that sounded like it was near my feet. I pretty much knew straight away what it was going to be caused by - the gearbox mount I’d made that secured the dump to the gearbox bellhousing.

Image description

Image description

Ever since doing that I’d read how it should’ve been done instead, i.e. with something that has a bit of give in it to allow for expansion/vibration/contraction. I had other priorities on the car as it was working, but now it was broken, I wondered what I should do? Patch it up and bung it back in? Take the car off the road for a bit, get it sorted and then be done with it for longer? I went with the latter, and it was off the road for probably 8 weeks total while I sorted that and some other stuff out.

Image description

I decided after a great amount of difficulty removing the flange bolts that I’d make v-band adapter to make it easier to service in future, as I had a leftover 3” aliexpress v-band from the last exhaust adventures. I got new locknuts and a couple of studs that got munted for the flange, too.

I asked around some places and ended up picking up two mandrel 90’s and a 45-degree bend in 3" from Pacemaker exhausts, who made it up to order, and when picking up I got to walk around their warehouse.. properly oldschool cool workshop - and huge. Nice to check out some local manufacturing.

Image description

With the bits in hand, I set off fabbing up the new dump, only keeping the turbo flange from the original dump. I used this as an excuse to get a small desktop belt sander to help me get the pipes matching up, and it was a huge help.

Image description

The turbine flange was really thick, so I welded that side from inside well, and die grinded it down, as well as from the outside once I'd cleaned up the surface.

Image description

I am not a professional welder, and my mates suggested a tshirt saying ‘a grinder and paint make me the welder I ain’t'. I lol’d.

Image description

As I got through it, I figured if I’m gonna make it nice, perhaps I should have it coated. I hate exhaust wrap, and figured it might be a good option. Pacemaker offer it as a service as well, and for $180 I decided to give it a go. It’s blasted and ceramic coated with a matte black finish inside and out, and came out looking pretty decent. They do a chrome coating finish for extra, but their most durable finish is the matte black so they say, and it's also the cheaper option. I have no need for bling on this, but the headers they make with that finish would look amazing on a shiny engine bay.

Image description

Image description

Image description

Got it installed and I’m happy with the result. One other thing I fixed up but didn't take photos of was the coolant hard line to the oil cooler that had been leaking for a while, so removed it, resealed the block and fitting and it's now no longer leaking. Huzzah. Was heaps easier to do without the dump in the way.

April 2024 - DIY Intercooler/Radiator/Condensor shroud

I was not happy with the radiator performance after installing the aircon a year or so ago - I was able to immediately notice that it was cycling the rad fan more, and could see from my UTCOMP that it was simply not getting the airflow it did previously.

After a lot of googling and thoughts, I came across some suggestions of using pipe lagging as a DIY method of sealing up between the sandwich of the 3 components, to force air through.

Image description

I thought I’d take it one step further and get some 6mm round steel stock from bunnings, bend it up to size with my old sheet metal brake, and weld it together after slipping on the pipe insulation.

Image description

I then glued the two ends of the pipe insulation together with contact adhesive designed for foam and other stuff and slot one in between the intercooler and rad, and the other in between the condensor and intercooler.

Image description

As for how it worked? It has worked so incredibly well. It only ever cycles the fan if it’s a warm day in traffic which is night and day compared to what it was before. A+++ would recommend. For less than $20 in materials and a little bit of time, I'm so glad I did it.

    March 2024 - PCV system diagnosis

    I’d been noticing some oil coming out of the oil filler cap and started to go down the path of diagnosing the PCV system function, which when tested, showed it clearly wasn’t working as expected. There was pressure coming out of the cap, but thankfully no oil leaks from elsewhere.

    All of the PCV system components were brand new as of 2020, about 16,000km ago, when I put the car together, but I decided to pull the breather box and check it out.

    I found out that the box was not sealed between the two halves of the box, and remembered back to a TB thread I’d seen mentioning that aftermarket boxes have often had this issue. Mine was from Skandix, but wasn’t volvo OEM.

    Image description

    Digging through a parts box, I found two Volvo OEM breather boxes, one seemingly completely clogged and the other one not seeming quite as bad. My guess is the clogged one is from the UK 940, and the other was on the Australian 1991 940.

    Image description

    Image description

    I decided to spend the next couple of days on and off cleaning it out as best I could, ‘til it consistently didn’t have anything coming out of it. I switched over the o-ring underneath and installed it, and while I still had a small amount of positive pressure on idle, as soon as it was off idle it would have a good vacuum down, so it was working again.‌ Time will tell if I continue to get oil out of the cap, but hopefully it'll be better from now.

    Supposedly the vacuum line off the hose-split above the box is supposed to assist with the vacuum on idle, though it doesn't appear to be clogged so.. *shrug. If anyone's got ideas about PCV efficiency at idle I'm all ears, or if I should just ignore it.

    It also seems to have solved a stumble that I was noticing more coming onto boost, that had been irritating me, so I’m glad it was able to fix that unexpectedly also!

    Check the nipple into the inlet manifold where the vacuum hose goes to for blockages, very common.

      This is something which I really need to sort out on The Cleever. She's had a broken oil trap box for as long as I've owned her, and it's getting annoying - the wagon interior becomes The House Of Pong with oil fumes during spirited driving.

      Years ago, when Yoshifab were doing their initial run of their crankcase vent plates, I bought 3 of them, but haven't fitted any of them yet.

      Image description

      The standard ones have a Dash 10 AN fitting (with a Dash 12 AN option) and a Dash 8 AN fitting for the return and are designed to be used with an oil catch can arrangement. The engines I'd planned to put them on were going to be used at high revs on the track, but track plans got shelved, and I still need to go shopping for a catch can / swirl pot arrangement which won't bust the bank. One of them is destined to go onto the 142's B230 16V+t engine when it gets done.

      I don't know yet if I'll put one of them on The Cleever's B230FT or not; depends what I find when I go shopping for a catch can for the Never-Ending 142 Project.

      ramrod

      Good shout - I did pull it off and inspect it as I was almost going to replace it, since the ones on the manifold are straight, don't have barbs and using silicon hose makes it hard to clamp the hose to without going nuts on the hoseclamp. Everything seemed clear there I think, but maybe I'll just double check in case I glossed over it.

      @Major Ledfoot - Give me a yell if you ever want to part with one of those 😃 I'd thought about going with the 'more proper' solution once I found this issue, but figured a free solution I had on hand would do for now. Ultimately I'd like a better, more easily serviceable PCV system like that, with a decent catch can.

      Clean box, JB Weld the two halves together, clamp it for 24h, will last for years. It does need to be properly clean though, for the epoxy to be effective.

      • deNs replied to this.

        Or, purchase a genuine oil trap, kill two stones with one bird as they say

          jamesinc
          In a similar tbricks thread I saw someone mention plastic 'welding' the box together with an old soldering iron to melt the two halves together, which I was tempted to do with an old iron, but right now as there's no immediate need I figured I'd leave it for now and think about what I want to do with it long-term. Thanks for the ideas though!

          ramrod
          Tempting, but I'm more likely to invest the coin in a better alternative and upgrade the PCV system with something else. I do wonder if using full synthetic oils make it less of an issue with clogging that in used to be - does anyone know?

          Changing the oil every six months keeps everything clean

          May 2024 - Additional Sound Insulation

          I installed a bunch of butyl sound deadener in late 2022, in an attempt to reduce some of the drone from the 3” exhaust. It made a small impact, but I wanted more, having lived with it in its current form for a while now. I could change the diff to a lower ratio for lower cruising revs, but… 4.10 is a lot of fun, ok?

          So, some Car Builders stage 2 insulation was in order.

          Image description

          With two rolls of the insulation, I did:

          • Front footwell up as far as I could get, about halfway up the firewall

          • Transmission tunnel

          • Rear footwell

          • Rear lower seat area

          • Also added some additional butyl deadener beforehand where panels still had some resonance

          It took a few days, and wanting more space, did it outside of the shed, which meant some rather cold late nights outside while doing this, but it’s fine. I did a bit of swearing when the paper back of this stuff kept tearing and being a pain, but it’s done now. Here’s the finished result:

          Image description

          After taking it for a drive, I immediately noticed a difference, particularly with regards to transmission noise - the rattly sound of the M90 was reduced noticably. I still have some noise reduction to do, and no, not replacing diff (yet).. but will be replacing the rear muffler. Also, I gave the car a wash. It was dirty.

          Image description

          You would only need a catch can with massive boost

          Plus proper install of one to imitate the original.

          3 months later

          June 2024 - New rear muffler

          Because the 10 year old within me knows that more exhaust pipes equals more power, I decided to double my power output and replace a single with twin tips. Besides the modified piping and cat converter this was the last remaining part of this hacked up JT-Tuning exhaust. I'm mainly doing it to further reduce cabin drone, and because I've never had a car with a shiny muffler and wanted twin tips.

          I don't own a TIG and right now don't intend to invest the coin into a new welder and learn on the muffler, so handed it to a local race fabrication shop which welded it in for a few dollarydoos.

          Muffler is a Vibrant, model 1111. 3 inch inlet, to twin 2.5" tips with straight stainless pipes welded on.

          Image description

          Gave the lower trim a lick of paint and mounted it up as best I could to ensure it was in the right place when the muffler was aligned.

          Also gave the rear bar a fresh coat of bumper black as it was looking a little shabby too.

          Image description

          Image description

          Image description

          Good enough for me! The bloke also helped me fix an issue where the axle was fouling on the pipe in one place under full compression so two birds one stone. I hadn't noticed but there were 'clearancing' marks on the pipe. Not terrible, but is good to fix.

          Has a nicer note now - didn't completely fix the drone, but it's a little better and I still have cards to play, in order to get the noise down.

          7 days later

          July 2024 - Fuel pump

          I backed out of our driveway one day and thought I’d stalled the car from not giving it enough revs, but then the car didn’t want to start back up. I could hear the main fuel pump running so figured it might be spark or ECU or something else..

          I was stuck diagonally across my road, and with the help of a neighbour and the starter motor, I got it off the road and back into the driveway.

          I tested injector firing to rule out CPS, ECU and injectors and tested a timing light on the spark leads, so my eyes turned to the fuel system.

          I'd read on a turbobricks thread that a failing lift pump can sometimes cause this issue, particularly when it's just under half a tank (which it was) so started looking at that.

          I tested the fuel pumps individually and both seemed to be working from what I could hear, and with no further diagnosis I consulted fellow 940 enthusiast @nugget_940 for advice after coming across his thread on the topic.

          Image description

          After some rather exuberant spreadsheeting in collaboration with him regarding parts required, I fired up the parts cannon and taking advantage of EOFY sales, got some shiny new parts for the fuel system, specifically:

          • Raceworks EFP-500 340lph E85-compat fuel pump

          • New E85 compatble hoses (5/16” and 1/2”) - (HPH-080-05M, RWH-400-08-1M)

          • New stock Ryco fuel filter (Z311)

          • Wiring bulkheads (FSA-499)

          • Fuel-safe heatshrink, wiring and fuel hose (FSA-095)

          • Fittings for fuel filter (RWF-731-06BK, RWF-732-08BK)

          • Barbs for fuel filter fittings (RWF-402-08BK, RWF-412-06-05BK)

          • Submersible 8mm hose - (Dayco 80160)

          With everything in hand, I started pulling the old stuff out and got a bit of a surprise.

          Image description

          Image description

          The in-tank fuel pump was replaced with a high-pressure unit at some point, likely when the previous owner turbo’d the car on the old engine before that was ripped out and the shell was sold to me. I was under the impression it was stock, and I put a high-pressure unit under the car. Turns out that’s probably been unnecessary the whole time, but meh. In-tank fuel hose was marked as 1995.

          Image description

          Image description

          Though the pump was upgraded to a high pressure unit, the 11mm fuel hose coming out of the tank was not rated for high-pressure, but was the original 0.05mpa (i.e. ~7psi) hose originally on the car. It was marked as 1993, so original, and was cracked at the ends. I’m pretty glad it didn’t burst and set things on fire.

          Image description

          Image description

          The old pump was removed from the hanger, and the Raceworks pump was installed, securing it with hose clamps in the original position. I tried using the plastic cage used on the bosch pump but I wasn’t happy with how it fitted. With the sock fitted, it was time to splice the wires to extend them to the bulkhead and plumb it all up before putting it in the tank.

          Image description

          It was then covered with fuel-safe raychem heatshrink.

          Image description

          Image description

          The raceworks high-current bulkhead connectors were installed after drilling two holes in the lid, and then it was all secured, ready for install.

          The old under-car fuel pump and filter were removed, and a new (stock spec) filter with the right AN fittings were installed in the original location.

          Image description

          Image description

          The new 5/16" (8mm) hose was then run up to the rail, and the return hose was replaced too. Everything except the hose connecting the rail to the reg is new, and I'll do that last piece shortly.

          Image description

          After some swearing, the carrier was installed back in the tank, new hoses were connected and the filter, and new feed/return lines were installed. It's a bit of a pain to run the new hoses to the hard lines near the tank, but I'm glad I did given the condition of the old main feed hose. Tank vent hose looked in fine condition so didn't replace it.

          I ran new 12AWG wire from the tank bulkhead connector all the way (~6 meters?) to the connector that originally powered the under-car pump.

          I put some new fuel in and it started up first crank, and no longer dies after moving around like it did. So far so good. Noticed there’s less power draw on the electrical system too with the voltage it sits at idling now. Clearly having two high-pressure pumps was putting a bit more load on it, and a single pump removes a point of failure so that’s nice.

          The best part? After some laps of the block, I realised the stumble I had coming onto boost is completely gone now, and it just freight trains. It’s completely different now I wonder how long it’s been on its last legs for. Very occasionally if I drop a gear and give it a boot my UTCOMP gauge would beep at me warning me of a lean condition (monitoring AFRs while in positive boost), at which point I immediately back off, but I thought it was possibly a lag between sensors. Fingers crossed that issue is solved too and that no damage was done to the engine because of that.

          After it was all buttoned up, I had an issue where the fuel level was stuck at the previous position, and immediately I thought it might be an issue with the float inside the housing that got stuck. I decided to brim the tank, go for a long drive in it and by the halfway point about 100km in, it had sorted itself out and reads properly again! Feels good.

          Edit: OH and there's even LESS cabin noise now, since that noisy-as-hell under-car pump isn't there anymore. I can't believe how much of a difference that alone made.

          I've fast great experience on my 740t using the gaz shocks that were -30mm shorter after my Bilstein hd's failed. Classic swede can supply them easily. I remember contacting king springs about Thier Springs for 7/9 models and they were 165lb, cutting them makes such a huge difference. But I'm also going coilovers when my 16vt is finished.

          Rip dump pipe! I'm glad the turbo is still going though!

          2 months later

          Aug-Oct 2024 - Diff Upgrades

          It started off innocently enough, a decision to seek some 3.73 gears to lower cruising revs and thus cabin noise..

          Then, since if I was going to change the gearing anyway, I bit the bullet on a TrueTrac and it was all downhill from there. I decided to give myself a couple of months to get this all sorted as I had no idea how long it was going to take.

          The short of it was the following happened:

          • Remove rear diff, take it to shop (I don't have the expertise, time or tools)

          • Install Truetrac, 3.73 gears, and BNE tone ring

          • Take out subframe and reinforce

          • Replace dogbone bushes with PU superpro items

          • Install BNE torque rods I bought years ago

          • Slam it back in the car again.

          Image description

          I picked up the torque rods and tone ring back in 2021 and had been waiting (checks calendar) a while to install them.

          Image description

          Thanks to @Samman88 , while I was back in Melbourne, I picked up a set of 3.73 gears off him and we talked Volvos and whatnot for a while. Thanks again!

          Image description

          Once the bloke I decided to go with was ready, out of the car the rear axle came. The guy I got to do the diff was great - the only wrinkle in the process was that inner tube axle seals were unavailable locally from my searchings, so an order to GCP had them here within a week, so only a minor setback.

          Edit: Oh! and for reference, the pinion seal was sourced from a bearing shop - SKF 15788. I also attempted to find the inner axle tube seals which were supposed to be SKF 14922 but I wasn't able to source these so that's why I went via GCP. There was also an equivalent National/Timken seal with number 1176 but I wasn't going to risk it given the local price was way more than sourcing seals via GCP.

          Image description

          Image description

          I reinforced the subframe using the same methods most people do on turbobricks when plating up their 7/9 subframes - with the exception that I didn’t plate the upper underside bit as I wasn’t totally sure where the torque rods travel and figure that plating it on the amount that I did, added a decent amount of rigidity. I did the tacks with the torque rods bolted in, and the initial one towards the front I tacked in while in the car so I had the widths correct.

          Image description

          I also carefully slotted, welded and ground back the fingers that slot into the dogbone so they’re not just a folded up piece as well.

          Image description

          Image description

          Image description

          Image description

          I got the same mob that did the tig welding for the exhaust to tack on the tone ring onto the housing, and they did a decent job. Welding it over the housing meant there was about a tooth gap, but it only reads a little under now, and with the spacer the diff guy put on it, it still reads, but I have to fix my speedo electronics still as it’s still as glitchy as it was.

          Image description

          Who knew they were red on the inside?

          Image description

          Image description

          Getting the dogbone bushes out had me wasting a couple of hours with jaw pullers and sockets an vices, until I just sawed one lip off and pushed it out. I didn’t want to wreck them, but I got fed up. New ones pushed in easily and they’re snug, so I’m happy about that.

          Image description

          Image description

          Bottom line - with the new gearing feels like this is what a M90L2 gearbox would have had from factory. I haven’t tested skids yet, and no additional NVH, so… win. It feels far less nervous while driving, which makes me less anxious behind the wheel, which is a huge plus. It wasn't a cheap endeavour, but I'm glad I'll hopefully never have to open it up again except for oil changes. I'm so glad this was done in time for nationals!

          10 days later

          Image description

          Well that should be attached..

          Upper panhard bolt ejected itself in rural NSW, limped it to the next town 15KMs away and sourced a bolt and got back on the road, torqued to 85Nm and lots of loctite.

          No issues today thankfully. Will post the rest of the details after nationals.